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基于滑模同步控制的履帶式作業(yè)機全向調(diào)平系統(tǒng)研究
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國家自然科學基金面上項目(51975253),、江蘇省自然科學基金項目(BK20210765),、鎮(zhèn)江市重點研發(fā)計劃項目(ZD2022002)、江蘇大學農(nóng)業(yè)裝備學部項目(NZXB20210101)和鎮(zhèn)江市科技計劃項目(CQ2022004)


Omnidirectional Leveling System of Crawler Machine Based on Sliding Mode Synchronous Position Control
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    摘要:

    針對現(xiàn)有丘陵山區(qū)履帶式作業(yè)機底盤大坡地作業(yè)時易側(cè)翻,、安全性差的問題,,基于“三層車架”式丘陵山區(qū)履帶式作業(yè)機結(jié)構(gòu)方案,設(shè)計了一種互聯(lián)式全向液壓調(diào)平系統(tǒng),,提出了基于擾動觀測器的滑模同步控制方法,,降低了單液壓缸位置誤差以及雙液壓缸同步誤差。AMEsim-Simulink聯(lián)合仿真結(jié)果表明:基于滑模同步位置控制的履帶式作業(yè)機全向調(diào)平系統(tǒng)優(yōu)于傳統(tǒng)PID控制,,全向調(diào)平中20°橫向調(diào)平時間減小1.6s,,25°縱向調(diào)平時間減小1.8s,上升時間平均縮短21.8%,,調(diào)平時間平均縮短35.5%,,同步位置控制誤差保持在±6×10-4m內(nèi)。在此基礎(chǔ)上,對3層車架式丘陵山區(qū)履帶式作業(yè)機樣機進行了實機測試,,其中全向調(diào)平機身傾角平均誤差為2.55%,,液壓缸平均同步誤差為8.2%,測試結(jié)果驗證了履帶式作業(yè)機全向調(diào)平系統(tǒng)的可行性與優(yōu)越性,。

    Abstract:

    Aiming at the problems that the chassis of crawler machine in hilly and mountainous areas is easy to roll over and the safety is poor, based on the developed structure scheme of “three-layer frame” crawler machine in hilly and mountainous areas, an interconnected omnidirectional hydraulic leveling system was designed to realize the pair-to-pair interconnection of four hydraulic cylinders in the upper frame that was horizontally levelled. The two hydraulic cylinders in the lower frame were connected in pairwise to realize longitudinal leveling. This system can make the center point of the crawler machine unchanged in horizontal leveling and longitudinal leveling. On this basis, a synchronization control strategy was proposed, which was based on the sliding mode synchronization control method based on disturbance observer. This method reduced the position error of single hydraulic cylinder and synchronous error of double hydraulic cylinder, and improved the stability of the system. The mechanical model of the crawler machine and the hydraulic model of the interconnected omnidirectional hydraulic leveling system were built in AMEsim, and the controller model was built in Simulink. The co-simulation results showed that the omnidirectional leveling system based on sliding mode synchronous position control was superior to the traditional PID control. In omnidirectional leveling, the 20° transverse leveling time can be reduced by 1.6s, the 25° longitudinal leveling time can be reduced by 1.8s, the average rising time was shortened by 21.8%, the average adjustment time was shortened by 35.5%, and the synchronous position control error was kept within ±6×10-4m. On this basis, the real machine test of the solid prototype of the “three-layer frame” crawler in hilly and mountainous areas was carried out. The average error of the tilt angle of the omnidirectional levelling body was 2.55%, and the average error of the hydraulic cylinder synchronization was 8.2%. The test results verified the feasibility and superiority of the designed omnidirectional levelling system of the crawler.

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汪若塵,蘇兆睿,丁仁凱,孫澤宇,蔣俞,郭中陽.基于滑模同步控制的履帶式作業(yè)機全向調(diào)平系統(tǒng)研究[J].農(nóng)業(yè)機械學報,2024,55(4):394-401. WANG Ruochen, SU Zhaorui, DING Renkai, SUN Zeyu, JIANG Yu, GUO Zhongyang. Omnidirectional Leveling System of Crawler Machine Based on Sliding Mode Synchronous Position Control[J]. Transactions of the Chinese Society for Agricultural Machinery,2024,55(4):394-401.

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  • 收稿日期:2023-09-07
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  • 在線發(fā)布日期: 2024-04-10
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